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Boat move went great. Helm is a little loose and over 15mph it gets hard to keep up with. The rudder post connections are tight, no slop so it must be at the front end of the system. I think these are chain and sprocket so maybe some stretch has occured. Very comfortable at 14mph turning only 1600 rpm. Here is some video..
http://youtu.be/8t_Hx4-1ELE
http://youtu.be/8t_Hx4-1ELE
- Stripermann2
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- captainmaniac
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I am a little surprised at the speed. Based on the wake, it does look like about 12-14 knots but I am surprised you got that at only 1500 rpm. My father's old '69 28' would be around 2000rpm to get that speed.
It's possible that they are different because of his being single engine, but if you haven't yet you may want to check the accuracy of your tachs.
It's possible that they are different because of his being single engine, but if you haven't yet you may want to check the accuracy of your tachs.
It was repowered in '91 with Crusader 230HP twins and propped 14X14. Next trip I will bring my optical tach and check but the numbers seem probable.captainmaniac wrote:I am a little surprised at the speed. Based on the wake, it does look like about 12-14 knots but I am surprised you got that at only 1500 rpm. My father's old '69 28' would be around 2000rpm to get that speed.
It's possible that they are different because of his being single engine, but if you haven't yet you may want to check the accuracy of your tachs.
As to how quiet, I was using a separate audio recorder placed on the helm area, then synced in post production (yeah I do video work on the side) so it brings the engine sound down. I'll get more video and capture the engine sound more accurately. They do sound great though!
I noticed the bilge pump ran much more often while running than when docked. Would that be prop shaft seals (it was the aft bilge pump).
- ready123
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Lightly (?) loaded twin woodie in salt water... seems possible to me.captainmaniac wrote:I am a little surprised at the speed. Based on the wake, it does look like about 12-14 knots but I am surprised you got that at only 1500 rpm. My father's old '69 28' would be around 2000rpm to get that speed.
It's possible that they are different because of his being single engine, but if you haven't yet you may want to check the accuracy of your tachs.
Michael
Rum is the reason Pirate's have never ruled the world
Done Dreamin'
1987 President 43' Twin Lehman 225SP Turbo
Highfield 310 Ally 15 HP Yamaha 2cycle
1978 F32 Sedan twin 318 Chry SOLD
Safe Cove Marina, Port Charlotte, FL
Rum is the reason Pirate's have never ruled the world
Done Dreamin'
1987 President 43' Twin Lehman 225SP Turbo
Highfield 310 Ally 15 HP Yamaha 2cycle
1978 F32 Sedan twin 318 Chry SOLD
Safe Cove Marina, Port Charlotte, FL
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I think Captain Maniac may be right; I have the same boat and run much slower at 1500 rpm. Also I find that when my boat is at rest the bilge never runs however after a weekend run and coming back to the slip if I turn the pump on manually it will pump some water out but it never gets enough in it to trip the float switch.
You may want to check and or replace your shaft log hoses; I know mine were shot when I got my boat.
Looks great on the water; congrats on your purchase.
You may want to check and or replace your shaft log hoses; I know mine were shot when I got my boat.
Looks great on the water; congrats on your purchase.
1963 31' Sea Breeze; Twin Interceptors
2000 21' Lightning; Marine Power 454 jet drive
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2000 21' Lightning; Marine Power 454 jet drive
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Simple flexing of the hull while underway may also let a bit in through seams that are otherwise tight when sitting at rest in the slip.Captain Blast Off wrote:after a weekend run and coming back to the slip if I turn the pump on manually it will pump some water out but it never gets enough in it to trip the float switch.
You may want to check and or replace your shaft log hoses; I know mine were shot when I got my boat..
Just got back from a weekend at the boat and updates on speeds and bilge.
I put a dwell meter/tach on the coil and the panel tach is within 50rpm of actual, so speeds/rpm are: 13mph @ 1500rpm, 28mph @ 2700rpm. Speeds are from GPS during slack water, maybe less than 1 knot of current. Incidently, the boat steered fine with just me on the boat. I think it is just VERY sensitive to weight shift as people move about the boat. I got it to 30mph in a burst and still tracked well.
I pulled the bilge hatches and the engine throughhulls are dry. The shaft hoses are wet, but forms it own little pool that does not contribute to the main seepage (leak is mostly forward, rear pump rarely runs). Forward pump triggers every two hours while in the slip and dumps about a gallon each time. I'm planning on bringing a wet vac and drying the bilge to find the culprit as I have no through hulls forward of the head. There rear pump runs when moving, but I think that is all the forward water draining to the rear.
Overall, a great trip. Did a lot of cleaning and made a list of varnishing I need to do. Got a short video of it on the Sacramento river I'll post tonight.
I put a dwell meter/tach on the coil and the panel tach is within 50rpm of actual, so speeds/rpm are: 13mph @ 1500rpm, 28mph @ 2700rpm. Speeds are from GPS during slack water, maybe less than 1 knot of current. Incidently, the boat steered fine with just me on the boat. I think it is just VERY sensitive to weight shift as people move about the boat. I got it to 30mph in a burst and still tracked well.
I pulled the bilge hatches and the engine throughhulls are dry. The shaft hoses are wet, but forms it own little pool that does not contribute to the main seepage (leak is mostly forward, rear pump rarely runs). Forward pump triggers every two hours while in the slip and dumps about a gallon each time. I'm planning on bringing a wet vac and drying the bilge to find the culprit as I have no through hulls forward of the head. There rear pump runs when moving, but I think that is all the forward water draining to the rear.
Overall, a great trip. Did a lot of cleaning and made a list of varnishing I need to do. Got a short video of it on the Sacramento river I'll post tonight.
Great looking boat!! Congratulations. I would be betting the water would be coming in around the keel. Shouldn't be too hard to find. I would guess all the floor boards are removable in the cabin. I had a leak in my 1965 36 at the forward keel. Not much of a leak at all sitting but underway, it was very obvious. Just got a buddy to man the helm and found it.
Good Luck
Good Luck